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Re: [TenTec] [SMC] OT: Half inch Andrews Heliax LDF4-50A vs LMR-400

To: "Discussion of Ten-Tec Equipment" <tentec@contesting.com>
Subject: Re: [TenTec] [SMC] OT: Half inch Andrews Heliax LDF4-50A vs LMR-400
From: "Bob McGraw - K4TAX" <RMcGraw@Blomand.net>
Reply-to: Discussion of Ten-Tec Equipment <tentec@contesting.com>
Date: Fri, 26 Apr 2013 07:03:08 -0500
List-post: <tentec@contesting.com">mailto:tentec@contesting.com>
One cause, typical thermal expansion and contraction caused by heating and cooling. The line strapped to the tower will have a different temp coefficient due largely to its black jacket while the tower which is steel and basically white.

73
Bob, K4TAX


----- Original Message ----- From: "Barry N1EU" <barry.n1eu@gmail.com>
To: "Discussion of Ten-Tec Equipment" <tentec@contesting.com>
Sent: Friday, April 26, 2013 3:35 AM
Subject: Re: [TenTec] [SMC] OT: Half inch Andrews Heliax LDF4-50A vs LMR-400


On Fri, Apr 26, 2013 at 1:36 AM, GARY HUBER <glhuber@msn.com> wrote:
I read a piece about
coaxial cable shields with aluminum foil and braided copper, repeated
flexing, and moisture which destroys the aluminum and is a diode action
noise source.


If you're not using it for the rotor loop, I don't see why a coax run
would be subjected to ANY, let alone repeated, flexing.

Barry N1EU
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